getting changed by "make ship" because the build is done in a place
where the path pointer to the user_id_programming GDS still points
back to the original caravel repository, not the user project
repository. The user_id_programming GDS was removed (no longer used),
the user_id_programming.mag file was modified to remove the path
pointer to the GDS, and the set_user_id.py script was modified to
make changes directly to the user_id_programming.mag file instead of
the GDS. An additional method was added to the set_user_id.py script
to modify the gate-level verilog/gl/user_id_programming.v to make
the user ID correct for gate-level testbench simulations.
it is exactly overlapping; this resolves issues with LVS. Also:
Corrected the references to the OpenLane/ path in the .mag files
by changing them to the canonical $PDKPATH reference.
to be abstract views, and modified the LVS scripts accordingly
(they no longer need a special version of the netgen setup
script). LVS was verified on both caravel and caravan using this
setup.
connections to the core side VCCD1 and VSSD1 on the clamped3 pads.
Also added scripts for running LVS on chip_io to the mag/ directory,
and revised the scripts so that they will only re-run extraction if
there is no netlist file in the mag/ directory.
(input for monitoring) changed from being connected directly to the
user project (where it shouldn't be) to the same signal on the input
side of the management protect block (where it should be). This is
functionally the same. Checked for any other signals connected
directly from the user project to any block other than mgmt_protect,
didn't find any (good). Modified the gate-level netlists and top-level
layouts for caravel and caravan with the corresponding change. This
was the only change affecting layout. Also: Revised the "pll"
testbench. This is still ongoing work. Also: Fixed the way the
pins on I/O pads are declared in chip_io.v, mprj_io.v, and pads.v, so
that it isn't so bizarre. Most of this change is functionally
agnostic (just a change in the way the ifdefs work), but did fix an
incorrect ifdef that causes the whole user power domain to be broken.
and open source logos. Modified the gpio_defaults_block layout
so that open holes are not created in the metal1 when the vias
are moved by the defaults block configuration script.
the clocking subcircuit from inside the pad area near the "clock"
pin to under the DLL. This prevents the DLL from having its
outputs travel all the way across the chip to reach the clocking
cell and then have the multiplexed clock travel all the way back,
especially as the DLL outputs are high-speed signals (up to 150
MHz).
update. Also changed the defaults block types in the layout so that
they match the gate-level netlist. This does not change the behavior
after assembly but lets LVS run correctly on the layout prior to final
assembly.
to housekeeping and the management core wrapper to separate the
wb_cyc_i signal and connect to new signal hk_cyc_o on the
management core. Also: Fixed a dangling input (user_clock) on
the housekeeping (minor error caused by the earlier refactoring
and unnoticed because there is no testbench covering that
function).
view pointing to the contents of ../gds/ so that when the assembled
chip's GDS is generated with "cif *hier write disable", the POR
will continue to have the GDS with the proper hierarchical processing.
to resolve the problem with the typo that caused the propagated
GPIO serial load, reset, and clock signals to get scrambled on the
user2 side. Caravel is now LVS clean again (Caravan needs layout
work).
verilog for both caravel and caravan. Hand-edited the RTL and GL netlists to
correct this; still need to correct the layouts. The error causes the user1
side clock, load, and reset buffers to drive the user2 side as well as the user1
side, making a huge mess of the routing. Will route this by hand.
Fixed rstb_h, which was being input to low-voltage blocks. (2)
Fixed flash_csb_ieb_core and flash_clk_ieb_core, which were not
output from housekeeping as they should be; the solution was
to tie the INP_DIS lines low at the pad by connecting them to
the TIE_LO_ESD line. This should probably be addressed in
housekeeping but would change the current pinout.
got removed from its net by a chang in the LEF view of an I/O pad, and
a lack of declaration of an array to attach to pwr_ctrl_out in the
verilog, which is valid verilog but netgen can't know the bus size
without the no-connect net being declared. The remaining issue has to
do with separation of ground domains in the mgmt_protect block.
so that it contains a valid layout after processing by Openlane (since the
verilog module is named gpio_defaults_block). Corrected the orientation of
the defaults block layouts on the right side of Caravel and erased the
incorrect routing there. Reinstated the copyright, user ID text, open source
logo, and Caravel logo. Revised the gen_gpio_defaults.py script to handle
the first five GPIOs in the same way as the others, although as fixed entries
which cannot be modified by the user project designer.
deleted "resetb_core_h" port label. Corrected the chip_io and chip_io_alt
verilog RTL files to replace the user area power supply clamp cells with
the new clamped3 cell from open_pdks.
layouts. Because the 1.8V domains are no longer within the pad
ring buses, they need to be connected together in the cell. These
internal lines were previously in the power routing cells.
verilog/rtl/, and creates all the layout files needed to represent
all unique combinations of defaults used in the file. Not done:
Modifying the top level layout to use the correct defaults (because
the top level layout does not yet exist).
three parameterized values used in the RTL verilog. Modified the
"user_defines.v" file to create verilog definitions that match the C-style
definitions from "defs.h", for convenience/simplicity.
continuous ring of vccd and vssd. The clamp connections for the
vccd1/vssd1 and vccd2/vssd2 pads still need to be done, although
the pads themselves have been changed to the base cell, matching
the new verilog RTL.
an unconnected wishbone bus (unconnected inputs). Added the missing
signals for the user IRQ enables to management protect (which have
to come from the management SoC).